Investor Presentaiton
TOTAL HELIUM
Engineering
Second Production Well: Miller 9D
Second project well 20 miles northeast of the
Boltz 35B well
Total drilling depth of 3,200 feet
5.5-inch production casing
80,000 lbs proppant
First stimulation performed on Miller 9D
compared to Boltz 35B
The smaller stimulation and limited entry
perforations were performed
150,000 lb. stimulation on the Boltz 35B led to
experimenting with a smaller stimulation on the
Miller 9D well.
Future stimulations will be designed with more
limited entry perforations and larger staged
stimulation
Second stimulation added 4 additional zones in
early May
80,000 lbs of proppant
Dewatering operations ongoing
Current production rate has increased from 20
Mcfpd and fluctuates between 100 to 300 Mcfpd.
Rate could increase with the dewatering process.
Initial production figures coming from only a
portion of total productive formations
Results from second stimulation ongoing and
expected to increase production.
Sales pipeline connected
Sales pipeline connected for helium, methane and
natural gas liquids
The gas sample show concentrations of 0.58%
helium, 61.01% methane and 3.09 gallons per Mcf
of natural gas liquids
Second Well: Miller 9D & Miller 9C
Miller 9C: Summary
Total Helium's 1st produced water disposal well
Very close proximity to Miller 9D allowing for
efficiencies and cost savings in drilling
Total depth of 6,200 feet
Proven disposal zone
High disposal capacity
5,000 bbls of water per day with 250 psig injection
pressure with current permitting
Well potential could be higher
Significant cost savings for disposal operations over
long periods of time
Connected to Miller 9D for dewatering operations
Currently taking 500+ bbls of water per day on a
vacuum
DUKE
DRILLING CO., INC.
RIG 1
Helium
0.58%
Nitrogen
26.28%
Methane
61.01%
Ethane
5.25%
Propane
3.34%
isoButane
0.38%
n-Butane
1.04%
isoPentane
0.21%
0.25%
0.34%
Nnpentane
Hexanes Plus
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